July-August 2010

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On the Cutting Edge

The first 15,000-ton, all-variable-frequency controlled chilling station

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By Juan M. Ontiveros

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The expected outcome from this approach would be that:

  • All online chillers would have identical flow and output through the evaporator.
  • All online chillers would have identical flow through the condensers.
  • Control valves on chillers would be line sized and open/close isolation only.
  • Chilled water supply temperatures could be reset (raised) when outside temperatures, and thus, cooling loads were reduced in order to improve chiller lift and energy efficiency.
  • Set up the automatic operation of the station in a way that guarantees equipment operational constraints are not exceeded
  • There would be no hunting or instability to chilled or condenser water temperature, flow, or pressure. 
  • Cooling tower water and chemical usage would be reduced, because the cooling tower could be operated at intermediate speeds other than just high and low speed.    
  • Part-load efficiencies and varying condenser water temperatures could be capitalized upon.
  • Chilling station efficiencies could be optimized for all load conditions.

Three modes of operation were designed into the controls strategy to address periods in which OptimumLOOP may not be working. This is described in Figure 6.

This planning led to a very successful project. The York Titan 5,000-ton chillers employed in this project are very efficient at peak kilowatt-per-ton efficiencies of around 0.60 kW per ton, with 85°F entering condenser water temperature. The campus was familiar with this equipment, as it owned two other York 5,000-ton chillers. The main difference is that the new chillers do not have gearboxes, and chiller loading is controlled via 4,160-V, 4,000-HP variable speed drives.

Prior to commissioning OptimumLOOP, the plant was operated without optimization for approximately six months to establish a before baseline. During this time, plant operation was tracked using OptimumMVM, the Web-based measurement, verification, and management service that is an integral component of the OptimumHVAC energy reduction system. The before baseline process established a total plant efficiency of 0.785 kW per ton, at 85°F, and the chiller was between 0.57 and 0.59 kW per ton, which met the requirement of the design-build contract.

With the OptimumLOOP optimization software in place, the Chilling Station 6 plant performance significantly improved.

  • In November 2009, the plant achieved 0.423 kW per ton with a load of 4,918 tons, an entering condenser water temperature (ECWT) of 61°F, and with outside conditions of an Outside Air Temperature (OAT) of 53°F, Outside Air Humidity (OAH) of 61% RH, and a Wet Bulb Temperature (WB) of 46.5°F.
  • Then, in January 2010, the total plant achieved 0.329 kW per ton with a load of 4,705 tons, OAT of 32°F, OAH of 51% RH, and WB of 30°F. This was totally unexpected and was a very pleasant surprise. It has become apparent that we do not have personnel (engineer or otherwise) that would always be able to make the correct set point decisions to take advantage of all changing conditions on a 24-hour, 365-day-per-year basis.

While we do not expect to see these kinds of efficiencies in the peak summer cooling season, it is possible we see improvement when temperatures are cooler at night. We hope to average approximately 0.50 kW per ton the entire year, which translates to $400,000–$500,000 savings for the year. Expected savings for the plant over the existing older plant was only about $140,000, plus $840,000 for the inlet air cooler. This was much better than anticipated. Figure 7 is a screenshot of the OptimumMVM dashboard on January 7, 2010. The blue line is actual performance, and the red is prior performance. On this day, the real-time savings was 63%.

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The OptimumMVM Dashboard view shows real-time plant energy reductions, daily and monthly dollars saved, and carbon dioxide reduction levels, and is one of many views available to measure, verify, and analyze plant and equipment performance.

In summary, it has become apparent to the University of Austin at Texas’s utilities organization that the paradigm of: “If you cannot measure it, you cannot manage it efficiently,” has changed to: “If you cannot measure it and model it, you cannot manage it efficiently.” We have learned that it is much less expensive to model processes, than to measure everything. A problem also develops when you gather a lot of data. It is difficult to see the right data and see its effect on the total system. We have applied this principle to our total plant, our chilled water distribution system, and now, our newest chilling station. We have used this knowledge to change the utility plant mindset, as illustrated in Figure 8.  


Author's Bio: Juan M. Ontiveros, P.E., is the Executive Director of Utilities and Energy Management at the University of Texas at Austin. In November 2008, Ontiveros was appointed to a National Research Council committee to help make the Capitol Power Plant in Washington, D.C., more energy efficient. He also served for three years as a judge for the ACEC Engineering Excellence Awards.

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