September-October 2008

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The University of Utahs new cogeneration project might look like any other system, but it represents an unexpected approach to CHP.

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CHP Unit

Photo: Chevron Energy Solutions The University of Utah contracted with Chevron Energy Solutions, in 1998, to replace its aging boilers with a new CHP unit

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By Ed Ritchie

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Due to the size of the campus, the heating system was designated as having upper and lower sections that were originally served by two separate boiler facilities. After weighing the issues of pumping hot water long distances and concerns about aging equipment, Chevron’s plan called for upgrading only the lower section.

“Initially we were hired to take a look at both heating plants and determine the viability of cogeneration,” Gallardo explains.  “Based on our analysis, we specified the lower campus heat plants as good candidates, but in the upper plants we recommended that they hold off until there was more heat load.” 

Photo: Chevron Energy Solutions

The new CHP unit's success has laid the ground-work for future improvements at the University.
As for handling future growth in the heat requirements of the lower campus, Chevron sized the turbine and waste heat unit to meet the demand for up to a 12% increase in heating loads. Conversely, when heating demands fall, the unit can be ramped down to operate in a “load follow” function. And with the university’s focus on sustainability, it’s likely that the turbine will see some days of below-average load demand. Although much of the university’s energy demand has dropped, thanks to the first five phases of Chevron’s energy savings contract.

Savings Rack Up Millions
In fact, the lowered demand was responsible for a surprisingly high financial impact on the total project. The unexpected excess savings from phase one were $780,000. Phase two saw excess savings of $620,000. The combined savings from the first two phases funded a new 6800-ton-capacity central chilled water plant. Phase 4 managed to deliver savings of $600,000—enough to pay for a new high-temperature water plant.

All these savings started with a comprehensive energy analysis launched in October 1998. The first and second phases addressed building energy usage in 24 buildings, with conservation improvements such as: high-efficiency lighting, new chillers, energy management systems, and variable speed drives and pumps. Phase three built a new 6800-ton chilled water plant. Phase four brought more energy conservation improvements to another 57 buildings, and phase five saw the construction of a 210-million-Btu-capacity, high-temperature hot water plant.

Chevron’s contract includes operations training for university personnel and the initial commissioning process will provide training on the waste heat recovery unit and the new controls for the plant. “Training and commissioning is a big part of what we're doing here,” says Gallardo.

Another big part is the contribution to a culture change. Gallardo has seen an impact far beyond the mechanical and electrical changes.

University president, Michael Young, agrees. “In everything we do there is not only a practical dimension, but there’s a teaching dimension as well,” says Young. “To the extent that we can weave into our everyday operations these habits and practices that make economical and environmental sense, it helps inculcate these principles into the lives of our students as they go out into the larger world.”

Now that phase six is drawing to close, Gallardo is taking a second look at both the complexity and the sheer volume of work. “One thing that is unique about working with a university is that they are huge,” he notes. “They have a lot of critical load and a lot of research is going on so any outage or inconvenience can be crucial. We had weekly construction meetings to review the previous week's progress and in addition to that to go over any issues coming up. The good communication has been a key factor in the project’s success.”

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For Higgins, success will be measured in the contribution to sustainability and the system’s economics. “We sized our project so that only 10 to 15% of our electricity will be generated by the unit, but 100% of our heat needs will be met,” he says. “It makes sense because we have to buy the gas to generate the heat either way and it's not that much more gas.”

Though the CHP unit was still waiting for final approvals from the utility company, initial estimates showed an increase of about 20% more natural gas over the amount used if the university had chosen to simply replace the old boilers with high-efficiency models. But much of that cost will be offset by the 6 MW of power, and one other factor that wasn’t a major issue until recently-skyrocketing oil prices. Next Page >

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